Well saturday night started out as a welded diff install....and turned into swapping the left front hub. And lemme tell you, my car needs anything but a welded diff. I went to Tom's (Didderson) and we jacked the car up off the ground.
Got another surprise to see that my oil feed line is lubing up every part of my car. I need to fix this pronto, so I'll have to yank the manifold AGAIN and fix this thing for good. I'm thinking OEM banjos with new crush washers, removing the braided lines. I havent made my mind up yet. So anyways back to the project. Tom was so anxious to use his welder and weld my bad studs up front so I could get the lugnuts off. I was trying to under the anti roll bar bolts, and I noticed every single rear bushing is cracked, dry rotted, and needs replaced. So energy suspension bushings are needed soon. So Tom begins welding and he welds the 2 studs we thought were bad. He goes and breaks those lugs loose and gave me false hope, thinking it was that easy. NOPE, turned out we welded the 2 good ones in place. LOL. So he began laying material the 2 bad ones. The first set of welds sucked, and they broke under a small amount of force. I was frustrated and Tom just continued to lay down beads of weld. Well, second time around, we let them cool longer, and Tom had increased voltage on one of the studs, needless to say, that one held and the lugnut came right off. So we knew we had to complete this. So about 2 hours later, the second one finally held with a tonnnn of material on it, and we had to make a trip to advanced auto. But here is a sight that brought on a celebratory brew.
So I had to get a 30mm socket for the wheel nut. Tom drove me out to advanced and we got it, came back and we figured it was a walk in the park from here.
NOPEEEE, this hub proved that it was not going anywhere, anytime soon. We tried with a 2 foot breaker bar, each of us laying on it with all our might, and we kept rocking the car all around and I was nervous that the car was going to fall off the stands so we stopped for a bit and thought about it. The next idea was taking the jack handle and putting it over the breaker bar and both of us pushing. LOL, no help, we even did our little engineering math, and figured we were putting a 500+ lb ft moment on this thing and the nut would not budge. Tom finally got an ingenious idea. Get the floor jack, and just jack up on the handle of the breaker bar. Needless to say, Tom made me do the jacking up, as the harbor frieght tool bent like it was plastic. I let it down and put the jack handle over top as a safety incase it exploded. I reset and tried again. I got the bar up pretty high and suddenly a large crack came out. Immediately I knew the tool broke, but amazingly it was fine. I didnt think it budged the nut but it infact did, because I reset and it worked and moved the nut again. Success, hub swap was easy from here on out.
UNTILLL, we noticed that the stock wheel bearing separated, and the backhalf was jammed into the spindle. Luckily with a flathead screwdriver and some BFH power, it popped off.
So on goes the new hub, torqued to 138 ft lb, and go to put the wheel on and what do you know, I still got an issue.
Some fuggin retard welded a steel washer inside the wheel thinking it would fix the hubs issue from before. So we had to drill that out. Drilled it out, and slapped the wheel on, put the new mutekis on and test drove. No wobbles, or out of balance issues. I do need new rotors though, as these would not pull away from the pads, they are sunk in really far, way past their effective life span.
Here's the finished product.
In the bottom right hole, you can see the washer thats welded in there, this is fine, because new wheels finally go on thursday. I have plans half the week and I need to help my parents out with some stuff wed, so I'll have another update soon. Rust repair is gunna happen soon too.