Post by
9sec240 »
https://forums.nicoclub.com/9sec240-u32495.html
Sun Apr 23, 2006 6:50 pm
What a crazy past 48 hours... My car has been on the dyno about 5 times, made a long road trip, hit the drag strip, and finally got named....
First off her new name is "Something Wicked" which she enjoys very much
Here is the run down of events...
As you remember, I was having boost creep issues with the small WG and large turbo... I swapped in a stiffer spring set to get base boost closer to where it crept to...
Yesterday (saturday):
She got strapped back on the dyno to try to get a good tune on 93 octane... With a 1.4 bar spring combo (21 psi) in the Tial 44, combined with colder weather, boost was creeping more than the previous dyno sessions... Swapping to a spring combo that was inbetween the 1 and the 1.4 bar spring sets didnt help either... unfortunatly Martin had to take off so the dyno session ended... I took this time to straighten out a few things on the car and swap in a .9 bar spring and got it strapped to the dyno for an early AM tune before heading off to Import Wars at Great Lakes Dragaway....
Today (sunday)
"Something Wicked" was looking all chipper strapped to the dyno at 7am this morning when I got to work... I had thought about things over night and decided that if the boost was creeping bad that a pump gas tune was just not going to cut it... Here is the issue... To keep the motor from knocking at the boost levels it was creeping to, timing had to be turned way down... Too little timing creates boost creep..... You can see in the dyno graphs I posted before that at over 5000 rpms, the graph gets choppy... This is one way to tell that the motor needs more timing... but with 93 octane, its going to detonate.... kind of a catch 22.... The first run on the dyno told the story... boost creep to over 25 lbs.. Time to drain the pump gas and put in some Street Blaze 101 in the tank... The only problem is that we are out of the 101 and the next step up is 110 octane... Oh well...
While Martin is tapping away on the computer changing the fueling and timing curves to somthing more appropriate for the race gas, I was pouring some really nice smelling purple VP racing fuel in the cell.... On the very first run you could see the difference... She really wanted some timing... LARGE power gains were made in the mid range and up top the graph was MUCH smoother... Boost only crept to 20 psi... Martin is a wizzard when it comes to tuning so it wasnt long before we finally got to turn the boost controler on
We needed to get a tune done kind of quick so I could take "Something Wicked" on our first date... I didnt want to be late and disappoint the girl by missing first round qualifying at import wars.... Turning the boost up to 25 netted some really decent HP... Things were looking really good... We ended up stopping at about 29 psi where she screamed out 550something HP to the wheels (dyno charts tomorrow).... We worked on the WOT shift tables.... Then some drivabiltiy on the dyno and then it was her time to shine...
With Chris1 behind the wheel and me behind the laptop, we ventured off on a 65 mile cruise to GLD... I was addressing part throttle shifting tables while Chris was fighting steering wheel shake... My bad.. I was very anxious to get the wheels mounted on my car when they came in that I just had the fronts mounted and didnt have them balanced... Anything over 70 mph on the expressway was enough to numb the hands and make all the mirrors useless... A 411 call later and we were headed to a Just Tires to get the tires taken care of... Its funny how small this world is some times... The Just Tires we ended up at just happen to have an fellow street racer working there who had me balanced up for FREE in about 20 minuets... I tipped him 20 bux and we headed off to Jewel to buy an I Pass (electronic toll paying device) because it was a real PITA to get money out when your strapped in with a 5 point harness....
On the highway she buzzed pretty loudly due to the solid motor and trans mounts but it was nothing unbearable... Everything worked like it was supposed to... Coolant temps at 189... IATs at 95... A/F right at stoich.... The only thing I was tweaking on the AEM was the shifting tables.... By the time we got to the track it was dialed in pretty damn well...
Tech was a breeze and after airing the tires down to 17 psi, I got into the staging lanes and waited for my turn... I just wanted to make a base boost run to make sure the car went straight, shifted like it should, and stopped well at the end... I wasnt expecting anything spectacular due to the lack of stall in the converter... I could only get about 2400 rpms out of it before I would push the front tires or brake the rears loose... I was predicting a 2.5 60ft and I ended up being a bit off... 2.54 seconds after I left the line I crossed the 60ft mark... She felt like a Nissan Quest minivan... about 330ft out, she was starting to get pissed... angry... violent.... out of nowhere, "something wicked" happend and she screamed as the open diff let the rear right tire spin... RPMs shot to 8000 and she banged second gear and spun the tire... BANG 8000 rpms and she slams into third... the tire stopped spinning... she squatted down in the back and lifted her front and we were off like a bullet.... Third gear is absolutly SICK... She pulls SOOOOOoooo hard.... My body is being pushed into the seat so hard as I cross the traps at 127 mph... She went straight as an arrow the whole way down the track... The brakes worked just like they should.... I pulled around to the timing tower and pick up my slip and its a 12.9 My car is the "OFFICIAL" poster car for turbo lag....
Second run is now with the boost controler on... I staged the Quest (I mean 240sx) and roll out to another 2.54 60ft... 330 come up and "Something Wicked" lives up to her name again... She changes shape right there on the track and becomes a SPORTS CAR!!!! Tire spinning, trans banging gears, WG roaring.... 131.5 MPH trap speed and I run 12.80 HAHAHAHAHAHA..... I heard that people were laughing in the stands and getting quite a kick out of my show.... Oh well.... She is going straight, shifting, and making power.... I have plenty of time to get the converter restalled... Another pass and she pulls a 12.7..... Last pass of the day... BAD tire spin at the top of first and all thru second and I went 13.5..... She is in one piece and ready to get some air in the tires for the trip home...
Well.. I am happy to report that she is safe at home nestled snugly in the garage waiting to show her wicked ways again at the turn of a key.... I am waiting for Ryan to finish the vids so that you all can see the violent temper of Something Wicked.....