Post by
shayandude »
https://forums.nicoclub.com/shayandude-u219395.html
Mon Apr 29, 2013 12:10 pm
Hey guys so I bought a 96 zenki with a s13 blk top in it. Car was dining super lean. So I put all new plugs, replaced the cracked exhaust manifold and elbow to a stock one. Took the hks actuator and out a stock 7 pound actuator on the car. Put a 255lhp fuel pump, new cts sensor, new z32 fuel pump. New o rings on the injectors. Car will run 15.5 to 17.5 at low rpm/ idle, and 13.1ish wot. I'm out of ideas of what to do or test next? Any idea guys? Anyone experience this before? I've also done a leak test, there was a tiny one by the t clamp and that's been fixed still not much better. Any idea or suggestions will greatly help. At this point I'm thinking dirty injectors or fpr? Thanks in advance guys.