Post by
kouki-gymkhana »
https://forums.nicoclub.com/kouki-gymkhana-u9464.html
Tue Jan 20, 2009 5:25 am
So, I've had my swap up and running (mostly) now for the past 3.5 yrs. I only drive the car very infrequently as it is really a play thing for me at this point. I've had numerous problems over the years...blown headgasket, broken camshaft...dead lifters....continued problems with cooling....etc and I'd just about given up on the car and decided to sell it. I've only put about 1500 miles on it since I completed the swap! For the past 6 months or so, the car had a serious stumbling problem around 3500rpm and would buck and hesitate like it was hitting a fuel cut. I though it might be a boost leak, coils going bad, R&R, etc. and I prepared my wallet for the worst ($$$).
I'm happy to report that after building a boost leak tester and getting off my kiester to diagnose the exact problem I've finally found the problem! As I was pulling the crossover pipe on my Hybrid FMIC piping kit, I pulled the T-bolt clamp on the side closest to the turbo and the bracket that bolts to the head and wouldn't you know the entire pipe just popped right off! That's right, the other end of the pipe wasn't tight at all! I felt like such an idiot! I buttoned everything back up super tight and now my baby runs like a beast! Idles super smooth, pulls HARD all the way to redline, and it looks like my super-duper fan arrangement is finally keeping the H20 temps in a good range (75-80C).
Sorry for the long post but I'm just so relieved that what I thought might be a serious problem has turned out to be the result of one loose T-bolt clamp on my IC piping!!
-KG