Post by
pirate87 »
https://forums.nicoclub.com/pirate87-u44619.html
Mon Sep 17, 2007 11:31 am
Shortly after putting the 1000th mile on my RB25-S14 swap, without a major issue, I decided I'd like to try to make it down to NOPI from my home in Durham, NC....about a 7 hour drive.
For a few weeks prior to the event, I monitored the car very closely and performed all routine mantinence. Everything was fine, as far as I could tell, so I set off with my buddy in his IS300 following. We'd been driving for about 2.5 hours and were just outside of charlotte when my PowerFC flashed the check engine light and the car bucked as if the fuel had been cut. Over the next 10 seconds this happened 4 or 5 times so I shot over to an exit ramp and parked it.
We threw the hood open and began to inspect the engine finding nothing out of the ordinary. I cranked the car and with a bit of coaxing (kicking the throttle) she started up and idled for about 5 minutes before cutting off again. We did this two more times and then decided to take it back out on the highway. After about 3 minutes of driving the bucking returned. Not being near an exit, I tried to drive through it, and eventually the car gave out while I was rolling ~50 mph. It was like the MAF had come unplugged while I was driving ( I have had this happen so I know the exact feeling), however the MAF plug was secure when we opened the hood. This time, there was no recranking the car. We waited and tried this every few minutes for about 1/2 an hour before deciding to call AAA.
To shorten an already long story, the car was towed back to durham and I continued on to NOPI with my buddy. Nopi was a great time, and returning home I plugged the car up to my FC datalogit (which I regretably did not pack, thus not data) and let it idle for a good 20 minutes. No problems. I had to drive to Raleigh (45 min drive) to return to school, so I decided to try the car......still not a problem.
When the problem happened, we were on the side of I85, and without the datalogit or a multimeter, the best we could determine was a MAF issue or something with the CAS....
my personal theory was that the maf collected too much moisture, as it had been raining the entire trip, and eventually just took a dump. Everything is fine now, but I still need to know what went wrong as to prevent it next time. Thanks for the input