well i dynoed my 90 coupe with ka24e. got one run out of it and then it crapped out. havent figured out what happend but the dyno results were much lower than expected. 130hp @ 6500 and 123ftlbs @ 4700. my torque curve is so flat. its almost at 123ftbls from 3100 to just over 5000. then it drops off slowly. it was dynoed on a mustang dyno. after the run was over, the car stalled. and shot alot of flaming **** out the back end. looked like gasket material. dont know why. but something really bad happened and i think it possibly blew the head gasket, but im going to tear into it and see what happened. if anyone has had a similar problem or might now what caused this then please feel free to chime in.
heres all the power adder i could think of, tell me what you all think:obx header, custom intake kyo exhaust 2.5 in test pipe port matched intake and exhaust magnecore wires beru silverstone plugs msd blaster 2 coil asp underdrive pulley obx adj fuel pressure regulator 300zx fuel filter walboro fuel pump 16in electric fan conversion removed secondary butterfly valves nismo motor mounts nismo transmission mount myth concepts tuned ecu removed ac (complete) myth concepts ground kit exedy stage 1 clutch i am running moble 1 synthetic in engine trann and diff if that makes a difference.
and i will link to the page with the dyno on it because its too large to post up here.
http://www.mythconcepts.com/We...1.jpg