ftp://240user:[email protected]/2 ... 20SRT4.MOV
Copy and paste the link to get the vid!
In video: I don't get 1 bar until 4900rpms and when I shift to the next gear, I have to almost completely respool (SUPER LAG!!!). Watch the boost gauge.
Well, having tuned the beast to 11-12 afr across the board (PLX Wideband/SAFCII) I somehow managed to screw up my motor.
After some test runs and a race...
I did a compression test and got 115,60,115,115,90,45 .....ouch.
I'm betting on blown rings, but maybe a headgasket? I ****-ton of smoke blew out in a race vs. a modded SRT-4 running 19psi. I was running 1 BAR.
Car won't idle on its own now. Also, I BLEW THE PCV VALVE OUT OF THE VALVE COVER AND OIL WENT EVERYWHERE....WTF???
Any ideas? My options so far are:
A. Rebuild the motor with forgies (CP pistons/Pauter rods) $3500B. Sell rb25, turbo, motor, crossmember, and all RB25 specific parts and acquire RB26 to run 400whp on stock injectors and rebuilt stock turbos. $8000-$RB25StuffSoldC. Hang myself.
Modified by accel junky at 8:50 PM 3/14/2005
Modified by accel junky at 8:50 PM 3/14/2005
Modified by accel junky at 8:52 PM 3/14/2005
Modified by accel junky at 8:53 PM 3/14/2005
Modified by accel junky at 8:53 PM 3/14/2005
Modified by accel junky at 8:54 PM 3/14/2005