WDRacing wrote:Check the compression for me real quick.
135, 145, 140, 135
biggie wrote:Some pics of the engine bay/ic/maf/bov setup may help as well.
Here ya go...
neverlift wrote:sounds like it could be blow out, coil might need a refresh, do the hotwire mod and see if it help(if it helps and doesnt fix it then the coil could be going) ka coils are generally a decent coil however it still a wear item.
well the fmu ~should be good~
try to drive it out of boost to 4.5k rpm(then get on it till 5.5k) if it hits vtech it could be the cts or knock sensor, on 12lbs I picked up like 50whp from bad knock sensor wiring... and that was a safe estimate.
Tried a friends known working coil. No difference. Found a loose ground, tightened it. Cleaned up ALL grounds. No difference.
Doesn't go into boost using the method you just described. I changed out the CTS and the knock sensor is brand new.
s13drifter88 wrote:the motor ran fine n/a and now it doesnt like boost. sounds like hes descibing a fueling problem. bad coil could cause some of his symptoms but the miss at idle sounds like it could be way rich and running out of steam at wot sounds like its leaning out. i think the stock maf is just freaking out for some reason. you could deff try another maf but im not entirely sure that will help. a turbocharged car will have a slightly more accelerated air stream passing thru the maf into the turbo. at idle your ecu thinks that your on the gas a little bit and as the turbo begins to make boost the maf is reaching max resolution and youre running outta gas. the fuel tables in the ecu of a factory turbo engine are programmed to see the faster air steam passing thru the maf at idle and can then correct it and of coarse has enough resolution to meter the intake air steam when on the gas at wot. i myself have never seen a ka run proper on all stock electronics when turbocharged. i know of many that have been boosted and run flawless on rom tunes with a larger maf. i could be wrong and there may be many that run great on stock electronics but none ive seen myself.
Coil is good. I tried a friends maf, no difference.
I disconnected the wastegate actuator arm from the turbo. Now when I floor it, it does go. It doesnt break up or anything, but of course it's at like 1 PSI with the actuator off. It STILL misses at idle...
I also pressure tested it again, and found a leak at the blow off valve flange. Fixed that. I also found that my fuel pressure regulator leaked during the pressure test...not from the vacuum line but like from the regulator itself. (These tests were at 20 PSI....my car only runs 7...)