I used a brand new infinity gasketI did gently bottom the adjuster and back it out 2.5 turns ( which is exactly where it started), At first I didn't mess with the adjuster, and then after high idle I set it and that wasn't the problem.I didn't miss a hose there was just the one large hose at the bottom which I checked and looked good.I did not squeeze the hose, although that should have been my logical nest step as my suspicion is that the aac is internally stuck open.I will try that first thing this morning.Thankssqueefoo wrote:Did you gently screw the adjuster all the way down and back it out ~2.5 turns?Miss a hose?Clean the connector contacts?Squeeze the 3/8" hose going up to #5 upper runner and see if the idle changes?
<shrug> LMK...
I didn't mess with the throttle body at allEngine was warm when I set iac bypass screw.I do have a plms interface that I can use when the time comes, but I am so far away from 675 rpms right now that I really don't need the laptop readout of rpms untill I can atleast get in the ballpark.Q45tech wrote:Remember even in summer you have the other circuit [the coolant temperature warm up idle cam] on throttle body. NEVER NEVER touch these as impossible to reset correctly once they have been turned from oem calibration.
You must make sure the engine is warm HAS BEEN RUNNING FOR 10 MINUTES before setting the idle rpm via the IAC air bypass screw.
You cannot trust tachometer when setting idle speed jard to resolve 25 rpm at 675.
My intention was not to clean again, but rather to inspect and then bench test with 12 volts to check for sticking of valve.I thought that sounded logical, but now I'm not so sure.Amyways, I also just replaced my transmission revolution sensor...While driving around this morning with no transmission malfunction message for the third day in a row (SWEEEEET it's fixed) I was really ripping hard and enjoying flawless shifts. To my pleasant surprise, when I park car rpms a tick above 600 (I will set with PLMS interface-laptop to ensure accurate rpms @ idle warm)I believe some of the old gasket fell into the AAC hose and got stuck in those close tolerances in the AAC. I noticed my oversight while scraping the old gasket off, but by the time I covered the hose it may well have been too late. If it does no reoccur I will stick with that conclusion, if not I may still bench test to check for nice stick free smooth operation, unless thats a stupid idea??My pcv valve is brand new as is my stock nissan air filter and my throttle body is clean, although I do need to clean all of the passages in the TB not sure of the condition. While I'm sure that is critical maintenance, I don't think it is related to my 1200 rpm idle that I was having as it idles perfectly until I disrupted the AAC. That is next on my list along with transmission fluid service tc rod bushings front upper links and then maybe a custom z32 diff.Q45tech wrote:I though you said you spent the hour with tiny tools [dental pics, etc microscope cleanroom] and multiple solvents cleaning ALREADY...............you will see the cylinder [valve] on the tip of solenoid arm and the close tolerances involved to get a fine resolution of air flow.
A work of art when it is clean and tuned precisely..................K&N sends oily dirt to IAC................I made that mistake 12 years ago.
Clean or replace the PCV valve and the output hose [and internal brush if so equipt].
If everything is not like brand new [spotlessly clean] the system cannot work like brand new!
You can watch duty cycle creep up and up and up as the miles since cleaning increase......................way to complicated a system for the typical car owner or typical technican of that era to TOTALLY comprehend.